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Home > Faults & Fixes > Air con |
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timmos Member Since: 20 Feb 2017 Location: Burton On Trent Posts: 22 |
I've just had mine re gassed yesterday after the recent spell of good weather. Mine was totally empty, had it re gassed, fully pressure tested and now its ice cold - yay,
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Fri Jun 02 2017 11:07am |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
dye put in but i know its not leaking as it had wey to much gas in it when we put it on the machine so no leaks i assume its either a switch or a relay |
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Fri Jun 02 2017 5:51pm |
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GodivaNige Member Since: 14 May 2016 Location: Warwickshire Posts: 420 |
Difficult to diagnose your problem online but it is the case that an overcharged system will eventually kill the compressor.
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Fri Jun 02 2017 10:28pm |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
Thanks for that but for 1 day after the recharge it worked absolutely fine and got really cold then stopped again |
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Sat Jun 03 2017 3:31am |
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GodivaNige Member Since: 14 May 2016 Location: Warwickshire Posts: 420 |
Have you scanned for faults? |
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Sat Jun 03 2017 6:27am |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
Can't see any in there I can see gas is in there as I think it was showing that there was pressure but not sure what it was is there anything in particular I should maybe look for |
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Sat Jun 03 2017 8:14am |
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Sharpy1980 Member Since: 24 Sep 2016 Location: Kent Posts: 98 |
Sometimes after regassing the schrader valves in the high and low ports can stick very slightly open much like on a car tyre valve which will then let the gas slowly come out even with the caps on, also there is a pressure sensor on the o/s on the pipework this shuts the system down if the pressure drops below 2bar or goes over (28bar I think it is), over gassing can be a misdiagnosis of a blockage in the system or more commonly a faulty expansion valve. It would depend on how the conclusion that it was over filled was made I.e from weighing the gas that was removed or from the readings on the manifold gauges?
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Sat Jun 03 2017 9:10pm |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
Hi the aircon machine in my friends garage told us that there was over 750 grams in there we took it out then put 600 back in when I looked with the idd tool I am sure the pressure was around the 500 mark but I would need to check again and confirm |
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Sun Jun 04 2017 5:24am |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
Ok must have a leak just used idd tool to check and it came up with low pressure or do i take to garage and see if there is gas in it as suggested to see if there is something else wrong as i said before it was gassed id did not work but then worked for a day after so i assume the compressor is working |
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Sun Jun 04 2017 10:03am |
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GodivaNige Member Since: 14 May 2016 Location: Warwickshire Posts: 420 |
You either have a leak and thus low refrigerant, or you have a blocked expansion valve due to insufficient vacuum prior to recharging.
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Sun Jun 04 2017 10:50am |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
Thanks will go back to the garage and extract the gas and see how much if any comes out |
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Sun Jun 04 2017 10:59am |
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GodivaNige Member Since: 14 May 2016 Location: Warwickshire Posts: 420 |
Yes, but the above needs to be carried out as described, just bunging gas back in without first correctly preparing the system is not only the 'cowboy' charge and hope method, but will more than likely not fix the problem. Insist your mate follows correct procedure. |
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Sun Jun 04 2017 11:05am |
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Sharpy1980 Member Since: 24 Sep 2016 Location: Kent Posts: 98 |
I checked my rrs with the iid today and mine shows the pressure as 7.2 bar with the a/c running, you need to check what measurement your iid is set to as it can be changed I.e bar ,psi or mpa I think. If it was over charged before then it is likely that it wasn't working previously so someone may have tried to add gas from one of those diy cans from Halfords etc.
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Sun Jun 04 2017 11:09am |
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geoffsnook Member Since: 19 Nov 2016 Location: cardiff Posts: 1699 |
Thanks for the info and i get where you are coming from so my first port of call is in fact see if there is any gas left in it and if there is then i have another issue so that is where i will start and if no gas it has dye in there so hopefully i will see where its got out |
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Sun Jun 04 2017 11:16am |
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